17 research outputs found

    Orbiter LH2 Feedline Flowliner Cracking Problem

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    In May of 2002, three cracks were found in the downstream flowliner at the gimbal joint in the LH2 feedline at the interface with the Low Pressure Fuel Turbopump (LPFP) of Space Shuttle Main Engine (SSME) #1 of Orbiter OV-104. Subsequent inspections of the feedline flowliners in the other orbiters revealed the existence of 8 additional cracks. No cracks were found in the LO2 feedline flowliners. A solution to the cracking problem was developed and implemented on all orbiters. The solution included weld repair of all detectable cracks and the polishing of all slot edges to remove manufacturing discrepancies that could initiate new cracks. Using the results of a fracture mechanics analysis with a scatter factor of 4 on the predicted fatigue life, the orbiters were cleared for return to flight with a one-flight rationale requiring inspections after each flight. OV-104 flew mission STS-112 and OV-105 flew mission STS-113. The post-flight inspections did not find any cracks in the repaired flowliners. At the request of the Orbiter Program, the NESC conducted an assessment of the Orbiter LH2 Feedline Flowliner cracking problem with a team of subject matter experts from throughout NASA

    Search for high-mass narrow resonances in virtual photon-photon interactions

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    Study of baryon correlations in e

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    Production of four-prong final states in photon-photon collisions

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    Pion and Kaon Pair Production in Photon-Photon Collisions

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    Exclusive production of proton-antiproton pairs in two-photon collisions

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    Pion and Kaon multiplicities in heavy quark jets from e+e− annihilation at 29 GeV

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    Study of η

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    Measurement of the Inclusive Branching Fraction τ

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